Interesting, also have a 69’ L78 CE engine that was completely redone but the little it run before tear down, same symptoms as 139tech, but would crank and run really well and then would run horrible and just quit. Had the 4346 gone over about 3 times, and same issues each time cranked. Engine man decided to pull 4346 and put new 750 Holley Quick flow and instant problem solved. Oh well 1 deviation from factory correct build of car well worth the cost. Don’t know if this helps, but my comfort still in the positive realm!